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FYI: Having rescued more than 300 of the Girling treasures (MK 2A mostly), I have seen any number of post re-build failures. The most recent cause of failure seems to be impatience. Almost a dozen have come back this year with jamming contaminations from the returning fluids. It seems that everyone is religious about flushing the master cylinder thru to the input line and making sure the fresh fluid fills the servo. But, a fresh servo boost loosens all that down stream nasty stuff inside the "out" lines and it washes back to cram the rear portions of the control & power valves to the point that it will all stop working. Take the time to completely flush those lines until clear guys & gals.